A few Quadra jet questions

Discussion in 'The Venerable Q-Jet' started by 70 GMuscle, Apr 24, 2020.

  1. 70 GMuscle

    70 GMuscle Plan B

    1 I have the edelbrock performer intake.
    It is a split divide at top.
    Which is the correct gasket.
    2i have a 1973 qjet. W divorced choke. Rod n spring. Is there an electric choke upgrade?
    3 has anyone had to add a washer to the primary throttle plate screw so the spring does not bounce around loose.
    I had the qjet built then repaired. It’s working better and will get back to it tomorrow.
    14* timing 33 total w mad distributor.
    It runs rough at idle but about 11” vacuum. Needs moves around a bit.
    I might add some questions tomorrow when working on it.
    Thank you.
     
  2. LARRY70GS

    LARRY70GS a.k.a. "THE WIZARD" Staff Member

  3. LARRY70GS

    LARRY70GS a.k.a. "THE WIZARD" Staff Member

  4. LARRY70GS

    LARRY70GS a.k.a. "THE WIZARD" Staff Member

    MAD distributor, you mean MSD? The engine might like a bit more initial. Are you using the largest (black) advance stop bushing?
     
  5. BuickV8Mike

    BuickV8Mike SD Buick Fan

    Why don't people like the divorced choke?
     
  6. LARRY70GS

    LARRY70GS a.k.a. "THE WIZARD" Staff Member

    Because the thermostatic spring eventually gives up the ghost, and they don't reproduce them.
     
  7. BuickV8Mike

    BuickV8Mike SD Buick Fan

    Very simple and dependable, except if the rod hangs up on the cover. ;)
     
  8. LARRY70GS

    LARRY70GS a.k.a. "THE WIZARD" Staff Member

    Yes, back to post #6. If you have to replace it, you might be SOL.
     
  9. 70 GMuscle

    70 GMuscle Plan B

  10. 70 GMuscle

    70 GMuscle Plan B

    Blocked heat crossover.
    Electric choke on holley worked fine.
    Trying to get qjet working I had built.
     
  11. 70 GMuscle

    70 GMuscle Plan B

    How is this?
     
  12. LARRY70GS

    LARRY70GS a.k.a. "THE WIZARD" Staff Member

  13. 70 GMuscle

    70 GMuscle Plan B

    Thank you Larry.
    I am going to contact him as I’m going to rebuild another qjet from my small collection.
    Great site he has.
    I read his book once. Getting a copy tomorrow to reread. There is info overload but I see many success stories. So I will give it another shot.
    The one I have has a whistle at idle down the primary Venturi. I checked w a I think they call it. Stethoscope.
    Noisy as can be there going at idle.
     
  14. 70 GMuscle

    70 GMuscle Plan B

    Had Buick out today. Cruise and response is excellent. Starting cold sucks. And when it gets fully heated it gets lean.
    So
    1 divorce choke hooked up. Works but very hard to get idle up to 1500 on ice cold. Need to help holdingctheottle or stuck in 1000 stinking up.
    2 gets real lean when idling to long. Turned mixture screws out 1/4 each seemed to help. 2.5 each now.
    3 whistle slight at idle. The throttle plate is barely cracked open at idle and timing at 14*.
    Carb was modified and over drilled I think.
    Not sure what will have to call and see.
    Still need to look int others I have saved.
    Drivability around is good but almost seems like it leans out at idle fully hot. Almost a shake when stopping.
    Tomorrow new day.need to hit the books.
     
  15. LARRY70GS

    LARRY70GS a.k.a. "THE WIZARD" Staff Member

    How do you know it's lean? Do you have an AFR gauge? Who did the carburetor?
     
  16. 70 GMuscle

    70 GMuscle Plan B

    Yes I have an A/F sensor.
    Carb built by Quadra jet power. My second failure from him. First had a completely corroded main body on bottom. Leaked fuel inside. Was in bad shape. Sent him 2 to build one. Received it and would not run. Mixture screws in op.
    Sent to Ken. Now runs but still issues. Dialing it in.
    Ken made an adjustment in idle circuit so yes it runs. I wanted him to run carb. Did not I believe.
    I will try to straighten out before calling him on advice. He is easy to reach.
    Qudrapower did not take calls last year which is why I sent to Ken.
    Ken fixed mixture to get runnable. But still missing something.
    Enough talk. I need to get back to work on it.
     
  17. 70 GMuscle

    70 GMuscle Plan B

  18. 70 GMuscle

    70 GMuscle Plan B

    Went back to open. Going for a road test.
     
    BuickV8Mike likes this.
  19. 70 GMuscle

    70 GMuscle Plan B

    No good.
    Pulled carb as I’m lost. Goes rich or lean and idle up sometimes.
    The fuel bowls are leaking into intake.
    Thru the pipe plugs. Also has fuel in port in front.
    I’m really disappointed.Drill and tap the plugs. I never question price If I’m comfortable as you need to make money. But darn. 2nd mess. I think the 2 ports in front were drilled my Ken. Idle bypass. Might be to big. I don’t know original size or what it should be. I got work ahead of me. And a sweet 70 350 replacement that ran 12.40. I will try to keep up this thread. Car has great response and will be track tested later in year.
    Timing is 16* initial at 35* total. which I’m surprised at as its biggest bushing. Thought it would be 22/35.
    Holley 780 going back to move car. lol.
     
    Last edited: May 2, 2020
  20. 70 GMuscle

    70 GMuscle Plan B

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